奥的斯ACD系列通用最新故障码(下)
使用服务器M1-1-2-1查看到的所有故障记录,所有事件类别分为I/W/F/EIInformation信息WWaring警告FFault错误EElite - Visible only in the ALL Menu Event TracesavedRuns从上次送电到现在的运行次数savedMins从上次送电到现在的时间(单位:分钟)

故障代码故障名称类别故障解释相关设置System0600SPB-AlertW服务面板检测到一个错误,需要手动救援SPB 和 SDI。可能的原因有:SDI 的错误的速度编码器SPB 上缺陷的 E2PROMSPB 上的电池缺失按SPB 按钮,REB+DDO 同时,以定位错误源控制板检测到 SPB 和 SDI 故障. Ssk 可能的原因有:1.编码器故障2.SPB 上的 E2 存储器故障3.电池故障同时按 SPB 上的 REB+DDO 定位故障原因Error # 1, encoder A failure (only ...AAA/...AAB)Error # 2, encoder B failure (only ...AAA/...AAB)Error # 4, E2Prom failureError # 5, battery failureError # 12, 3 encoder A failureError # 13, received out of range parameters fromTCBC/GECB /RCBII0601SPB:TempHTSW服务面板过热。SPB-Temp0602LwssServiceW称重板请求REM。参见称重板故障原因。称重系统请求服务0603Aro ServiceWThe ARO subsystem (modified SPBC_III) requested “Request For Service” (REM). See AROsubsystem’s event logging for reason.0604S/WChangedI软件变更。SCN 更改0605Update S/W!F升级软件!要求更新 GECB 软件0606SpbServiceWSPB 请求服务0607/TUM1FTUM1 missing after run at TOP or active during standstill; (reduced overhead: trig- ger modulcontacts)TUM1(1047)HWY-TYP0608/TUM2FTUM2 missing after run at TOP or active during standstill; (reduced overhead: trig- ger modulcontacts)TUM2(1048)HWY-TYP0609/TDMFTDM missing after run at BOTTOM or active during standstill; (shallow pit: trig- ger modul contacts)TDM(1049)HWY-TYP0610/TUPSFTUPS missing during run; (reduced overhead: trigger modul power supply)TUPS(1050)HWY-TYP0611/TDPSFTDPS missing during run; (shallow pit: trigger modul power supply)TDPS(1051)HWY-TYP0612SOS upFSafety Operated Switch Up triggeredSOSU(1054)HWY-TYP0613SOS downFSafety Operated Switch Down triggeredSOSD(1055)HWY-TYP0614PRBB BatLowWThe battery of the PRBB board is weak: During PowerOff, the battery only pro- vides power forless than 10 seconds.EN-PRBB=10615PCB CertiWThe PCB certification is not performed by using OEK PDA until the specified days expired. In orderthat this function is ap- plied, it should be set by OEK PDA. Note: only for Korea application0616C-circuitFC-circuit does not work correctlyNote: only for MCS310C-CHK (704)0617RBU-SelftstFSelftest of Rope Brake has failed (i.e. lasted longer than 5 seconds).Car is blocked until TCI/ERO is switched.RBTC (1029)RBTE (1028)0618RBU-FaultFRope Brake has detected overspeed. Car is blocked until TCI/ERO is switched.RBTC (1029)RBTE (1028)0619HWY-TYPFPlease refer to blinking message “LOPIT cfg!”Low Pit0626DeepBatteryFLVA Switch or Evolux: Deep Discharge Protection switched off the OCB to pro- tect the batteries(voltage was < 40 VDC).GECB-LV DRV-TYP0627LowBat waitFLVA Switch or Evolux: Enforced Battery ChargingGECB_LV DRV-TYP0628NoPowerWaitFLVA Switch or Evolux: BatRun-T expired during blackoutGECB-LV DRV- TYPBatRun-T0629HighBatWaitFLVA Switch: Enforced Battery Discharg- ingBattery voltage exceeded 70 VAC.GECB-LV0630OverBatFLVA Switch: Overvoltage Protection is going to switch off the OCB to protect the batteries(voltage > 75 VDC).GECB-LV0631E2P MappedIThe LCB2/TCBC E2Prom data, provided by an E2TB (E2prom Transfer Board) were mapped to theGECB layoutevent0701SP missingFNode Guarding does not detect the SP at the CAN bus. Check CAN_OK LED at SP;Check CAN wiring between GECB & SP;0702BCB missingFNode Guarding does not detect the 1st BCB at the CAN bus. Check CAN_OK LED at LVPB/BCB_IICheck CAN wiring between GECB & LVPB/BCB_II0703BcbIoFailFThe state of inputs was not received eve- ry second or the output command was not acknowledged.CAN bus overload?Defect LVPB/BCB_II?0704BcbHwFailFThe BCB published an EEPROM error.Exchange LVPB/BCB_II0705BcbSwFailFThe BCB published a task timing prob- lem.See subcode 'x’ for detailsExchange LVPB/BCB_II according to subcode0706EncoderFailFThe rescue encoder generates no signals during a normal run. Check rescue encoder wiring;Replace rescue encoder or GECB_II;0707OCB failFThe OCB auxiliary contacts are wired incorrectly. Check wiring to OCB;Check OCB;Check GECB_II inputs;0708OverspeedWThe measured rescue encoder speed is 15% faster than the nominal speed. The OS contact or the safeties could be acti- vated. MRO is prevented.Reset OS contact;Check Encoder / Speed parameter;SPEEDEncoder0709MRO_BRK FltFA wrong voltage at the brake was detect- ed.That means that the brake could be unin- tentionally lifted during MRO. Check input MRO_BRK and wiring of the brakeCheck LVPB / Replace LVPBDO NOT PERFORM MRO!!!LVA0710No BatteryFThe 1st BCB misses the rescue battery.Check RPS / battery0711BatTempErrWThe 1st BCB indicates that the battery cannot be charged, because the tempera- ture is out of range.Check battery temperature sensor注:删除单个故障:服务器 GO ON 或者 GO BACK 选中将要删除的故障SHIFT(蓝健) + 1 (ON) 然后 SHFIT + CLEAR (ENTER) 当前单个故障删除新版本有 M1-1-2-7菜单,代替了SHIFT(蓝健)+UP(2 )了解详细的清除主板故障步骤在公众号里找:奥的斯服务器查看主板故障清除故障
